This airplane
was manufactured
at Lockheed in
1961. This
plane was
acquired on
October 01,
1962. The
planes
assignment was
VMGR-352.
This Story
was Written by
LtCol. Donald E.
Cathcart and
Submitted by
David Joyal
BLACK SHEEP TEST
HOP
"Another day
in which to
excel!" I
shouted. "I
deeply regret
that I have but
one life to give
for my Corps and
Country!"
Greg Sloan, the
VMA-214 squadron
scheduling
officer, then
started a fiasco
by popping his
head into my
office and
asking, "Major
Mofak! Do you
want to fly a
post-maintenance
test hop? The
Skyhawk is ready
and there are no
other test
pilots
available."
"Sure Greg. We
need every
possible
aircraft
op-ready to meet
your tough
flight
schedule. Tell
the wrench
benders that
I'll be at the
line shack as
soon as I change
into my zoom
bag." As the
Black Sheep
Operations
Officer, I was
glad to oblige
maintenance.
The troops were
busting their
buns to provide
planes to train
our replacement
pilots for
Vietnam. Up to
four young
pilots were
transferred each
month to combat
squadrons in
Vietnam.
Peaceniks called
replacement
pilots cannon
fodder.
Many pilots
would not return
home.

The maintenance
history of the
Douglas A4C was
laid out in the
line shack for
my perusal prior
to accepting the
bird for test.
I found nothing
unusual in the
yellow sheets.
One pilot had
commented,
"Engine makes
night noises in
the daytime."
Quality Control
had signed off
on the plane.
The Skyhawk was
also signed off
by Corporal
Barbeau, the
Plane Captain.
The Aircraft
Maintenance
Officer, Major
Darrell Shelor,
had initialed
all entries and
thereby approved
the test flight.
Normally, pilots
were famous for
"kick the tire
and light the
fire" on the
aircraft they
were to fly. A
test hop
required a
closer
examination of
the aircraft
since the
fuselage had
been taken apart
and the engine
replaced.
Engine removal
entailed
disconnecting
hydraulics,
electrics, fuel,
and other
systems from the
old engine and
then
reconnecting all
systems to the
new engine. The
Skyhawk took
about ten
minutes for
pre-flight
inspection. All
systems appeared
to be "Go." I
climbed up the
eight foot
ladder and
checked the
ejection seat
for
discrepancies.
Finding none, I
dropped into the
seat which
housed the raft
and survival
gear. The plane
captain strapped
me into the seat
and removed the
safety pins from
the ejection
seat firing
mechanism.
After climbing
down he carried
the ladder to
the start cart.
The plane
captain got me
started and
completed the
taxi checks. He
pulled the
chocks, then
saluted and I
taxied toward
the runway.
El Toro tower
personnel
cleared the
aircraft for
takeoff and
departure to
Whiskey 291 for
completion of
the test
flight. I
shoved the
throttle forward
on the J-65
engine and
watched the RPM
and EGT rise to
takeoff power.
With all gauges
indicating
normal, I
released the
brakes and felt
the surge of
thrust as the
Skyhawk
accelerated down
the runway. The
exhilaration of
becoming
airborne in the
sleek little jet
thrilled me just
like it did the
very first
time. "OoooooooRaaaah!"
W-291 was the
military
training area
south of
Catalina
Island. Except
for Navy and
Marine fighter
aircraft
rolling, looping
and tumbling
after each other
while
dog-fighting,
the warning area
was a safe place
to operate
without worry of
commercial or
private aircraft
interference. I
finished most of
the test card
above 25M and
descended to
15,000 feet to
perform the
flight controls
disconnect. The
radio became
quiet. I called
departing W-291
but received no
response.
Checking other
frequencies, I
discovered the
radio had
failed. I
decided not to
disconnect the
controls and
extend the stick
without a
radio. Another
quick test hop
would be
required for
that test item.

The El Toro
weather was VFR
with no clouds
and 10 miles
visibility. I
flew up the
entry channel
and entered the
break at 1500
feet. I rocked
my wings
repeatedly to
alert tower
personnel that
the aircraft had
no radio and
required a green
light for
landing. I
rolled rapidly
into a 60 degree
bank and pulled
the Skyhawk
around 180
degrees to the
downwind. I
moved the
landing gear
handle to the
down position.
The main gear
indicators
flipped from 'up'
to
barberpole and
then to down and
locked. The
nose gear
position
indicator
flipped to
barberpole and
stayed. The
tower was
shining a green
light. The
unsafe nose
landing gear
position
indication, the
wheels warning
light and the
red warning
light in the
gear handle
meant no landing
for a while.
The fuel gauge
indicated 2200
pounds. Kiss a
fighter pilot's
ass! Some days
a pilot
shouldn't don
his zoom bag! I
executed a wave
off and departed
the traffic
pattern.
I climbed above
10,000 feet and
began
trouble-shooting
the landing gear
system.
Recycling the
gear up and back
down did not
provide a nose
gear down
indication. I
put the gear
handle down and
applied positive
G forces to lock
the gear. No
joy! I
increased the
airspeed up to
350 knots which
was the limit
for forcing the
nose gear aft
into the locked
position. When
that attempt
failed, I pulled
the Emergency
Gear Extension
Handle. Still
the nose gear
indications
remained unsafe.
The landing gear
problem created
an urgent need
for the radio.
Turning switches
on and off,
resetting
circuit breakers
and re-plugging
connections
produced no
joy. I dumped
cockpit
pressurization.
The earphones
crackled! Aha!
The radio
operated
intermittently
with no
pressurization.
I transmitted my
dilemma to the
control tower.
Using the
sporadic radio,
I arranged for
Black Sheep
maintenance
personnel to be
at the approach
end of the
runway to
inspect my nose
gear as I made a
low pass. I
also advised the
Tower that my
fuel was below
1000 pounds. A
KC-130 was
awaiting
takeoff. The
crew called, "We
can takeoff and
give you fuel
from a drogue.
We can visually
check your nose
gear while you
are taking
fuel." "Click!
Click!" I
replied, "Let's
do it!"
The KC-130 took
off to the south
and within a
minute I joined
on his left
wing. I
reported,
"Stabilized port
side. Fuel 800
pounds." The
KC-130 crew
extended the
port drogue and
cleared me to
take fuel. The
refueling crew
chief called,
"The nose strut
looks vertical
and normal for
landing."
I plugged the
Skyhawk probe
into the
refueling
drogue. The
radio receiver
went dead. The
green receiving
fuel light on
the refueling
pod did not
illuminate even
though the hose
had been pushed
up to 15 feet
from the pod.
Just what I
needed--another
SNAFU! I flew
the hose in and
out of the pod
trying for the
refueling
light.
Suddenly, the
hose rapidly
unreeled
completely out
of the refueling
pod. Whipping
violently, it
wrapped around
the nose of the
Skyhawk. I
chopped power to
get away from
the drogue but
it remained
connected to the
probe while the
hose stayed
coiled around
the refueling
probe, my canopy
and the forward
fuselage. The
end of the
flapping hose
trailed behind
my aircraft.
The routine test
hop had really
become a can of
worms!
I broke away
from the tanker
toward El Toro.
My fuel state
was only 500
pounds and now I
was carrying a
drogue with
about 80 feet of
refueling hose
flailing the
sky. I pointed
the nose of the
plane at the
touch down point
on the runway
from my position
at 1200 feet and
5 miles on final
approach. I
dropped the
tailhook. The
tower showed me
a green light.
They obviously
recognized a
regurgitating
fecal sandwich
in progress. I
touched down on
the main gear
and held the
nose off the
runway until
crossing and
engaging the
arresting gear.
The troops ran
out and inserted
the gear safety
pins. I shut
down the engine
with about 10
minutes of fuel
remaining. The
troops began
unwrapping the
hose from the
fuselage and
disconnecting
the drogue from
the refueling
probe. They
hooked a TUD-80
to the Skyhawk.
It looked like
they wanted to
ready the plane
for another test
hop. But first
they had to work
off the serious
gripes that I
entered on the
yellow sheet.
Maybe I would
skip the next
test hop on A4C
Buno 147755.
Mofak
Back to Back We
Face the Past
A Special Thank
You to Alan
Deegan Who
Worked to Get
These Stills
From an 8mm
Movie Shot in
DaNang, SVN.
Thanks Again
Alan


In 1970 at MCAS
El Toro, while
training, this
airplane crashed
and burned.
This crash was
well know to all
of us that lived
on the base.
We lost friends
in this crash.
My brother
Robert and I,
along with Bill
Palmers kids
were in the
river bed near
base housing
when this
occurred.
We immediately
ran for home to
see what had
happened.
We found Bill
Palmer's wife on
the phone, with
mom listening
closely.
No information
was given, and
we all loaded up
in Bill's
Chevrolet
Corsair and
headed to the
commissary
parking lot.
We had a good
view of the
flight line from
their.
Real heavy smoke
and allot of
Marines
scrambling
around to see.
We knew Frank
Smith was on a
training flight
that day.
We could not
find dad, and
there was no
answer at his
office at the
130 school where
he taught.
This plane sat
upside down on
the runway's end
for quite some
time. That
is all I can
remember of this
crash.
The training I
believe was
short approach
training.
The airplane went
into an
unrecoverable
stall and became
upside down on
the runway.
There were some
survivors in
this accident.
Anyone with
stories about
this plane are
encouraged to
send them to
Nick for
postings. Also
any other
photo's of this
plane or the
crew's that flew
her.
Nick@kc130.com |